HAND CRANK GENERATOR
Some
of the printers I'd been taking apart contained DC motors instead of the
steppers I was mainly after. Hewlett Packard ones and anything intended
for high resolution or photo printing tend to use DC motors along with
an optical fringe band or disc position sensor so as to get a better resolution
than can be obtained with steppers. I decided I ought to do something with
them, and one day I got an Epson 300 photo grade printer which contained
a printhead drive belt long enough to fit over a small spare bicycle
wheel (when you build pedal generators you tend to get front wheels
left over). I found a spare bit of front fork to mount the wheel using
a coachbolt as a spindle and jigged it up
on a piece of scrap metal for a base. The belt
and motor from the printer looked as if they'd fit. I made a mounting
plate for the motor and welded it to
a bit of tube. Some brackets for a pivot
were made up and then welded to the base.
The motor was fitted and the setup tested
with a small light bulb.
In any project involving putting together bits of recycled
stuff there's at least one stage where it looks as if it's all gone wrong,
and I'd just hit that stage. I hadn't noticed before but the teeth on the
motor gear (and the belt that came with it) were actually slightly angled,
and the load of the light bulb pushed the belt sideways against the end
washer nearest the motor and it fell off
taking the belt with it. One answer might have been to reverse the rotation
direction or turn the motor mounting around. The first option might have
made it more acceptable to the proportion of the population (including
me) that are left handed, and the second one would have meant re-doing
the whole thing in mirror image.
The solution I found was to rummage around in the box
of motors, getting this one which had straight
teeth and a solid rim at one end of the gear. The gear was a tight push
fit on the spindle so it was easily reversed to put the rim on the motor
side. Of course, this motor was a different size so the mount was modified
and welded back together.
The generator worked well with the new
motor and a small spring from the printer to tension the belt. The
fact that the belt still had angled teeth didn't seem to matter at all
and it would easily run small light bulbs without slipping. In any case
the generator was only meant to produce a couple of Watts and the motor
which probably originally ran on 24V had a winding resistance of about
four Ohms.
A handle was quickly fabricated
from bits of folding pushchair (one of the most useful things you can get
off the rubbish tip) and braced to the wheel
hub using a bit of printer rod. The whole thing was given a coat of paint
and fixed to an offcut of chipboard as a base with a recycled christmas
tree light as an output indicator. Final modifications were a pair of output
sockets and a Schottky diode (from the printers power supply) in series
to prevent reverse polarity if it was turned the wrong way.